clack
04-10-2014, 19:35
Hi everybody, a couple of months ago I have been contacted by a fellow that has been lucky enough to obtain from Transcriptors a Spyder turntable, not before the usual waiting and struggle.
The turntable he received had all the problems described by many before.
http://www.vinylengine.com/turntable_forum/viewtopic.php?f=36&t=36262&p=573494#p573494
It is not possible to run it at the right speed, no matter if 33 or 45, beyond very strong speed fluctuations.
In a word, it was unusable.
Once the turntable has been checked, it was obvious that the power supply could not give the voltage needed by the motor to run correctly. Mechanically it had an excessive slack for all the parts that should be of the most precision, in order to allow the table to turn correctly and sound the way it should.
The first part of the job regarded the power supply, that had the modification needed to give the motor the voltage it needs to run correctly at both speeds.
After that, the power supply has been given a mains switch, so the inner parts do not remain connected to the mains all the time, followed by a fuse placed before the transformer, just to comply the usual safety rules.
A last touch regarded placing a blue led behind the speed selector. So it remains hidden but its light is reflected nicely by the metal panel, indicating when the power supply is on.
The mechanical part of the job was the hardest. First of all there has been to find a workshop that accepted to do the work, something that seems not so easy nowadays.
After a long search I found a guy who works professionally with lathes, patient enough to complete the work the way it needed.
First he checked with his gauges and verified that between the frame and the pivot assembly there was a slack of more than half a millimeter.
So we began making on the main frame a new seat for the lower part of the spindle assembly, the one inside which the bearing ball is placed. The spindle assembly itself needed to be completely rebuilt in all of its parts: the lower that goes inside the main frame, the upper that supports the platter and a new brass bushing as well.
The spindle originally supplied with the turntable was clearly bended, so also for it a rebuilding has been made.
This has been the most difficult part of the mechanical job: we had to build two spindles before obtaining the precision that I wanted.
Now the spindle, when left placed in its seat, remains up and needs some help to get all the way down, till it touches the bearing ball.
When it is pushed down after the obvious lubrication of the parts involved, not only the air inside the receptacle offers a remarkable resistance, but it is possible to hear it getting out, such is the precision of the parts.
Even when the spindle is pulled out a resistance is experienced, caused by the difficult entering of the air into the pivot seat.
Now the turntable is able to keep the correct speed even after many hours of working, both at 33 and 45 RPM, without audible fluctuation.
Equipped with a Rega RB 250 tonearm and a Nagaoka MP 200 cartridge sounds remakably well, with an ease of informations recovering and an authority worth of more revered machines.
http://i61.tinypic.com/2552oic.jpg
Here the turntable after refurbishing
http://i60.tinypic.com/20h7xgp.jpg
New spindle assembly and seat with the original ones on the left
The turntable he received had all the problems described by many before.
http://www.vinylengine.com/turntable_forum/viewtopic.php?f=36&t=36262&p=573494#p573494
It is not possible to run it at the right speed, no matter if 33 or 45, beyond very strong speed fluctuations.
In a word, it was unusable.
Once the turntable has been checked, it was obvious that the power supply could not give the voltage needed by the motor to run correctly. Mechanically it had an excessive slack for all the parts that should be of the most precision, in order to allow the table to turn correctly and sound the way it should.
The first part of the job regarded the power supply, that had the modification needed to give the motor the voltage it needs to run correctly at both speeds.
After that, the power supply has been given a mains switch, so the inner parts do not remain connected to the mains all the time, followed by a fuse placed before the transformer, just to comply the usual safety rules.
A last touch regarded placing a blue led behind the speed selector. So it remains hidden but its light is reflected nicely by the metal panel, indicating when the power supply is on.
The mechanical part of the job was the hardest. First of all there has been to find a workshop that accepted to do the work, something that seems not so easy nowadays.
After a long search I found a guy who works professionally with lathes, patient enough to complete the work the way it needed.
First he checked with his gauges and verified that between the frame and the pivot assembly there was a slack of more than half a millimeter.
So we began making on the main frame a new seat for the lower part of the spindle assembly, the one inside which the bearing ball is placed. The spindle assembly itself needed to be completely rebuilt in all of its parts: the lower that goes inside the main frame, the upper that supports the platter and a new brass bushing as well.
The spindle originally supplied with the turntable was clearly bended, so also for it a rebuilding has been made.
This has been the most difficult part of the mechanical job: we had to build two spindles before obtaining the precision that I wanted.
Now the spindle, when left placed in its seat, remains up and needs some help to get all the way down, till it touches the bearing ball.
When it is pushed down after the obvious lubrication of the parts involved, not only the air inside the receptacle offers a remarkable resistance, but it is possible to hear it getting out, such is the precision of the parts.
Even when the spindle is pulled out a resistance is experienced, caused by the difficult entering of the air into the pivot seat.
Now the turntable is able to keep the correct speed even after many hours of working, both at 33 and 45 RPM, without audible fluctuation.
Equipped with a Rega RB 250 tonearm and a Nagaoka MP 200 cartridge sounds remakably well, with an ease of informations recovering and an authority worth of more revered machines.
http://i61.tinypic.com/2552oic.jpg
Here the turntable after refurbishing
http://i60.tinypic.com/20h7xgp.jpg
New spindle assembly and seat with the original ones on the left